[B1758] Replace Lars EVT with DVT |
||||
Issue descriptionSteps: Verify device (asset tag: C073530) powers on and boots Switch to dev mode Set gbb_flags for fast boot Install ToT test image Add servo cable Install in android1758-row4-rack3-host2 Run network_WiFi_VerifyRouter in B1758 Run platform_InstallTestImage in B1758 Return Lars EVT
,
May 24 2016
Servo is pingable and servod process is running but platform_install test is failing for some reason. ping android1758-row4-rack3-host2-servo.cros PING android1758-row4-rack3-host2-servo.cros.corp.google.com (100.107.127.99) 56(84) bytes of data. 64 bytes from dhcp-100-107-127-99.mtv.corp.google.com (100.107.127.99): icmp_seq=1 ttl=60 time=0.982 ms 64 bytes from dhcp-100-107-127-99.mtv.corp.google.com (100.107.127.99): icmp_seq=2 ttl=60 time=0.826 ms ^C --- android1758-row4-rack3-host2-servo.cros.corp.google.com ping statistics --- 2 packets transmitted, 2 received, 0% packet loss, time 1001ms rtt min/avg/max/mdev = 0.826/0.904/0.982/0.078 ms ps -ef | grep -i servod root 1615 1 0 00:28 ? 00:00:00 /usr/bin/python2.7 /usr/lib/python-exec/python2.7/servod --host 0.0.0.0 --board lars --port 9999 root 1622 1586 0 00:28 pts/0 00:00:00 grep --colour=auto -i servod 7:21:01 INFO | Began logging to /tmp/test_that_results_bMB7TC Adding labels [u'cros-version:ad_hoc_build', u'board:lars'] to host android1758-row4-rack3-host2.cros 19:21:01 INFO | Fetching suite for job named platform_InstallTestImage... 19:21:04 INFO | Scheduling suite for job named platform_InstallTestImage... 19:21:04 INFO | ... scheduled 1 job(s). 19:21:04 INFO | autoserv| Results placed in /tmp/test_that_results_bMB7TC/results-1-platform_InstallTestImage 19:21:04 INFO | autoserv| Logged pid 1211 to /tmp/test_that_results_bMB7TC/results-1-platform_InstallTestImage/.autoserv_execute 19:21:04 INFO | autoserv| I am PID 1211 19:21:04 INFO | autoserv| Not checking if job_repo_url contains autotest packages on ['android1758-row4-rack3-host2.cros'] 19:21:04 INFO | autoserv| Processing control file 19:21:04 INFO | autoserv| Starting master ssh connection '/usr/bin/ssh -a -x -N -o ControlMaster=yes -o ControlPath=/tmp/_autotmp_EWgvD9ssh-master/socket -o StrictHostKeyChecking=no -o UserKnownHostsFile=/tmp/tmp6ELvky -o BatchMode=yes -o ConnectTimeout=30 -o ServerAliveInterval=300 -l root -p 22 android1758-row4-rack3-host2.cros' 19:21:06 INFO | autoserv| Pinging servo host at android1758-row4-rack3-host2-servo.cros 19:21:08 INFO | autoserv| Pinging host android1758-row4-rack3-host2-servo.cros 19:21:08 INFO | autoserv| Starting master ssh connection '/usr/bin/ssh -a -x -N -o ControlMaster=yes -o ControlPath=/tmp/_autotmp_47uLgfssh-master/socket -o StrictHostKeyChecking=no -o UserKnownHostsFile=/dev/null -o BatchMode=yes -o ConnectTimeout=30 -o ServerAliveInterval=180 -o ServerAliveCountMax=3 -o ConnectionAttempts=4 -o Protocol=2 -l root -p 22 android1758-row4-rack3-host2-servo.cros' 19:21:09 INFO | autoserv| Host (ssh) android1758-row4-rack3-host2-servo.cros is alive 19:21:09 INFO | autoserv| Applying an update to the servo host, if necessary. 19:21:09 INFO | autoserv| servo host android1758-row4-rack3-host2-servo.cros does not require an update. 19:21:10 INFO | autoserv| servod is running, PID=3491 19:21:10 INFO | autoserv| Attempting to repair servo host android1758-row4-rack3-host2-servo.cros. 19:21:10 INFO | autoserv| START ---- reboot timestamp=1464049270 localtime=May 23 19:21:10 19:21:10 INFO | autoserv| GOOD ---- reboot.start timestamp=1464049270 localtime=May 23 19:21:10 19:22:04 INFO | autoserv| [stderr] mux_client_request_session: read from master failed: Broken pipe 19:22:05 INFO | autoserv| [stderr] Warning: Permanently added 'android1758-row4-rack3-host2-servo.cros' (RSA) to the list of known hosts. 19:22:05 INFO | autoserv| [stderr] Warning: Permanently added 'android1758-row4-rack3-host2-servo.cros' (RSA) to the list of known hosts. 19:22:06 INFO | autoserv| Master ssh connection to android1758-row4-rack3-host2-servo.cros is down. 19:22:06 INFO | autoserv| Starting master ssh connection '/usr/bin/ssh -a -x -N -o ControlMaster=yes -o ControlPath=/tmp/_autotmp_syP_3zssh-master/socket -o StrictHostKeyChecking=no -o UserKnownHostsFile=/dev/null -o BatchMode=yes -o ConnectTimeout=30 -o ServerAliveInterval=180 -o ServerAliveCountMax=3 -o ConnectionAttempts=4 -o Protocol=2 -l root -p 22 android1758-row4-rack3-host2-servo.cros' 19:22:07 INFO | autoserv| GOOD ---- reboot.verify timestamp=1464049327 localtime=May 23 19:22:07 19:22:07 INFO | autoserv| END GOOD ---- reboot kernel=3.8.13 localtime=May 23 19:22:07 timestamp=1464049327 19:22:27 INFO | autoserv| Pinging host android1758-row4-rack3-host2-servo.cros 19:22:27 INFO | autoserv| Host (ssh) android1758-row4-rack3-host2-servo.cros is alive 19:22:27 INFO | autoserv| Applying an update to the servo host, if necessary. 19:22:28 INFO | autoserv| servo host android1758-row4-rack3-host2-servo.cros does not require an update. 19:22:28 INFO | autoserv| servod is running, PID=623 19:22:28 INFO | autoserv| Failed to repair servo: [Errno 111] Connection refused 19:22:28 INFO | autoserv| Exception escaped control file, job aborting: 19:22:28 INFO | autoserv| Traceback (most recent call last): 19:22:28 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/server_job.py", line 684, in run 19:22:28 INFO | autoserv| self._execute_code(server_control_file, namespace) 19:22:28 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/server_job.py", line 1182, in _execute_code 19:22:28 INFO | autoserv| execfile(code_file, namespace, namespace) 19:22:28 INFO | autoserv| File "/tmp/test_that_results_bMB7TC/results-1-platform_InstallTestImage/control.srv", line 72, in <module> 19:22:28 INFO | autoserv| parallel_simple(run, machines) 19:22:28 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/subcommand.py", line 93, in parallel_simple 19:22:28 INFO | autoserv| function(arg) 19:22:28 INFO | autoserv| File "/tmp/test_that_results_bMB7TC/results-1-platform_InstallTestImage/control.srv", line 37, in run 19:22:28 INFO | autoserv| host = hosts.create_host(machine, servo_args=servo_args) 19:22:28 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/hosts/factory.py", line 160, in create_host 19:22:28 INFO | autoserv| host_instance = host_class(hostname, **args) 19:22:28 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/hosts/base_classes.py", line 58, in __init__ 19:22:28 INFO | autoserv| super(Host, self).__init__(*args, **dargs) 19:22:28 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/client/common_lib/hosts/base_classes.py", line 70, in __init__ 19:22:28 INFO | autoserv| self._initialize(*args, **dargs) 19:22:28 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/hosts/cros_host.py", line 306, in _initialize 19:22:28 INFO | autoserv| try_lab_servo=try_lab_servo) 19:22:28 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/hosts/servo_host.py", line 789, in create_servo_host 19:22:28 INFO | autoserv| required_by_test=required_by_test) 19:22:28 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/hosts/base_classes.py", line 58, in __init__ 19:22:28 INFO | autoserv| super(Host, self).__init__(*args, **dargs) 19:22:28 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/client/common_lib/hosts/base_classes.py", line 70, in __init__ 19:22:28 INFO | autoserv| self._initialize(*args, **dargs) 19:22:28 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/hosts/servo_host.py", line 173, in _initialize 19:22:28 INFO | autoserv| self.repair() 19:22:28 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/hosts/servo_host.py", line 708, in repair 19:22:28 INFO | autoserv| '\n'.join(errors)) 19:22:28 INFO | autoserv| ServoHostRepairTotalFailure: All attempts at repairing the servo failed: 19:22:28 INFO | autoserv| [Errno 111] Connection refused 19:22:28 INFO | autoserv| INFO ---- ---- timestamp=1464049348 job_abort_reason=All attempts at repairing the servo failed: [Errno 111] Connection refused localtime=May 23 19:22:28 All attempts at repairing the servo failed: 19:22:28 INFO | autoserv| [Errno 111] Connection refused 19:22:28 INFO | autoserv| Starting master ssh connection '/usr/bin/ssh -a -x -N -o ControlMaster=yes -o ControlPath=/tmp/_autotmp_vcbHVmssh-master/socket -o StrictHostKeyChecking=no -o UserKnownHostsFile=/tmp/tmpr5t4Y7 -o BatchMode=yes -o ConnectTimeout=30 -o ServerAliveInterval=300 -l root -p 22 android1758-row4-rack3-host2.cros' 19:22:29 INFO | autoserv| Starting master ssh connection '/usr/bin/ssh -a -x -N -o ControlMaster=yes -o ControlPath=/tmp/_autotmp_2NZaCYssh-master/socket -o StrictHostKeyChecking=no -o UserKnownHostsFile=/dev/null -o BatchMode=yes -o ConnectTimeout=30 -o ServerAliveInterval=900 -o ServerAliveCountMax=3 -o ConnectionAttempts=4 -o Protocol=2 -l root -p 22 android1758-row4-rack3-host2.cros' 19:22:30 INFO | autoserv| Collecting crash information... 19:22:30 INFO | autoserv| There are no orphaned crashes; deleting /tmp/test_that_results_bMB7TC/results-1-platform_InstallTestImage/crashinfo.android1758-row4-rack3-host2.cros 19:22:30 INFO | autoserv| android1758-row4-rack3-host2.cros already up, collecting crash info 19:22:30 INFO | autoserv| Collecting /var/tmp/messages.autotest_start... 19:22:30 INFO | autoserv| Collecting /var/log/messages... 19:22:30 INFO | autoserv| Collecting 'dmesg' ... 19:22:30 INFO | autoserv| Collecting /var/log... 19:22:30 INFO | autoserv| Collecting /dev/pstore/console-ramoops... 19:22:30 INFO | autoserv| trying scp, rsync failed: Command <rsync -L --timeout=1800 --rsh='/usr/bin/ssh -a -x -o ControlPath=/tmp/_autotmp_2NZaCYssh-master/socket -o StrictHostKeyChecking=no -o UserKnownHostsFile=/dev/null -o BatchMode=yes -o ConnectTimeout=30 -o ServerAliveInterval=900 -o ServerAliveCountMax=3 -o ConnectionAttempts=4 -o Protocol=2 -l root -p 22' -az --no-o --no-g root@android1758-row4-rack3-host2.cros:"/dev/pstore/console-ramoops" "/tmp/test_that_results_bMB7TC/results-1-platform_InstallTestImage/crashinfo.android1758-row4-rack3-host2.cros/console-ramoops"> failed, rc=23, Command returned non-zero exit status 19:22:30 INFO | autoserv| * Command: 19:22:30 INFO | autoserv| rsync -L --timeout=1800 --rsh='/usr/bin/ssh -a -x -o ControlPath=/tmp 19:22:30 INFO | autoserv| /_autotmp_2NZaCYssh-master/socket -o StrictHostKeyChecking=no -o 19:22:30 INFO | autoserv| UserKnownHostsFile=/dev/null -o BatchMode=yes -o ConnectTimeout=30 -o 19:22:30 INFO | autoserv| ServerAliveInterval=900 -o ServerAliveCountMax=3 -o ConnectionAttempts=4 19:22:30 INFO | autoserv| -o Protocol=2 -l root -p 22' -az --no-o --no-g 19:22:30 INFO | autoserv| root@android1758-row4-rack3-host2.cros:"/dev/pstore/console-ramoops" "/tmp 19:22:30 INFO | autoserv| /test_that_results_bMB7TC/results-1-platform_InstallTestImage/crashinfo.an 19:22:30 INFO | autoserv| droid1758-row4-rack3-host2.cros/console-ramoops" 19:22:30 INFO | autoserv| Exit status: 23 19:22:30 INFO | autoserv| Duration: 0.037220954895 19:22:30 INFO | autoserv| 19:22:30 INFO | autoserv| stderr: 19:22:30 INFO | autoserv| rsync: link_stat "/dev/pstore/console-ramoops" failed: No such file or directory (2) 19:22:30 INFO | autoserv| rsync error: some files/attrs were not transferred (see previous errors) (code 23) at main.c(1637) [Receiver=3.1.1] 19:22:30 INFO | autoserv| rsync: [Receiver] write error: Broken pipe (32) 19:22:31 INFO | autoserv| Collection of /dev/pstore/console-ramoops failed: scp -rq -o ControlPath=/tmp/_autotmp_2NZaCYssh-master/socket -o StrictHostKeyChecking=no -o UserKnownHostsFile=/tmp/tmpqLRMhs -P 22 root@android1758-row4-rack3-host2.cros:"/dev/pstore/console-ramoops" '/tmp/test_that_results_bMB7TC/results-1-platform_InstallTestImage/crashinfo.android1758-row4-rack3-host2.cros/console-ramoops' 19:22:31 INFO | autoserv| * Command: 19:22:31 INFO | autoserv| scp -rq -o ControlPath=/tmp/_autotmp_2NZaCYssh-master/socket -o 19:22:31 INFO | autoserv| StrictHostKeyChecking=no -o UserKnownHostsFile=/tmp/tmpqLRMhs -P 22 19:22:31 INFO | autoserv| root@android1758-row4-rack3-host2.cros:"/dev/pstore/console-ramoops" '/tmp 19:22:31 INFO | autoserv| /test_that_results_bMB7TC/results-1-platform_InstallTestImage/crashinfo.an 19:22:31 INFO | autoserv| droid1758-row4-rack3-host2.cros/console-ramoops' 19:22:31 INFO | autoserv| Exit status: 1 19:22:31 INFO | autoserv| Duration: 0.196501970291 19:22:31 INFO | autoserv| 19:22:31 INFO | autoserv| stderr: 19:22:31 INFO | autoserv| scp: /dev/pstore/console-ramoops: No such file or directory 19:22:31 INFO | autoserv| Collecting /sys/kernel/debug/dri/0/i915_error_state... 19:22:32 INFO | autoserv| Traceback (most recent call last): 19:22:32 INFO | autoserv| File "../third_party/autotest/files/server/autoserv", line 547, in run_autoserv 19:22:32 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/site_server_job.py", line 65, in run 19:22:32 INFO | autoserv| super(site_server_job, self).run(*args, **dargs) 19:22:32 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/server_job.py", line 684, in run 19:22:32 INFO | autoserv| self._execute_code(server_control_file, namespace) 19:22:32 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/server_job.py", line 1182, in _execute_code 19:22:32 INFO | autoserv| execfile(code_file, namespace, namespace) 19:22:32 INFO | autoserv| File "/tmp/test_that_results_bMB7TC/results-1-platform_InstallTestImage/control.srv", line 72, in <module> 19:22:32 INFO | autoserv| parallel_simple(run, machines) 19:22:32 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/subcommand.py", line 93, in parallel_simple 19:22:32 INFO | autoserv| function(arg) 19:22:32 INFO | autoserv| File "/tmp/test_that_results_bMB7TC/results-1-platform_InstallTestImage/control.srv", line 37, in run 19:22:32 INFO | autoserv| host = hosts.create_host(machine, servo_args=servo_args) 19:22:32 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/hosts/factory.py", line 160, in create_host 19:22:32 INFO | autoserv| host_instance = host_class(hostname, **args) 19:22:32 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/hosts/base_classes.py", line 58, in __init__ 19:22:32 INFO | autoserv| super(Host, self).__init__(*args, **dargs) 19:22:32 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/client/common_lib/hosts/base_classes.py", line 70, in __init__ 19:22:32 INFO | autoserv| self._initialize(*args, **dargs) 19:22:32 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/hosts/cros_host.py", line 306, in _initialize 19:22:32 INFO | autoserv| try_lab_servo=try_lab_servo) 19:22:32 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/hosts/servo_host.py", line 789, in create_servo_host 19:22:32 INFO | autoserv| required_by_test=required_by_test) 19:22:32 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/hosts/base_classes.py", line 58, in __init__ 19:22:32 INFO | autoserv| super(Host, self).__init__(*args, **dargs) 19:22:32 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/client/common_lib/hosts/base_classes.py", line 70, in __init__ 19:22:32 INFO | autoserv| self._initialize(*args, **dargs) 19:22:32 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/hosts/servo_host.py", line 173, in _initialize 19:22:32 INFO | autoserv| self.repair() 19:22:32 INFO | autoserv| File "/mnt/host/source/src/third_party/autotest/files/server/hosts/servo_host.py", line 708, in repair 19:22:32 INFO | autoserv| '\n'.join(errors)) 19:22:32 INFO | autoserv| ServoHostRepairTotalFailure: All attempts at repairing the servo failed: 19:22:32 INFO | autoserv| [Errno 111] Connection refused 19:22:32 INFO | autoserv| 1 19:22:32 INFO | autoserv| Traceback (most recent call last): 19:22:32 INFO | autoserv| File "../third_party/autotest/files/server/autoserv", line 769, in main 19:22:32 INFO | autoserv| File "../third_party/autotest/files/server/autoserv", line 561, in run_autoserv 19:22:32 INFO | autoserv| SystemExit: 1 19:22:32 INFO | autoserv| record_state_duration failed: job_or_task_id=None, hostname=android1758-row4-rack3-host2.cros, status=Running ----------------------------------------------------------------------------- /tmp/test_that_results_bMB7TC/results-1-platform_InstallTestImage [ FAILED ] ----------------------------------------------------------------------------- Total PASS: 0/1 (0%)
,
May 28 2016
,
Jun 29 2016
Lars DVT has been running test successfully. Closing this. https://wmatrix.googleplex.com/platform/wifi_matfunc?platforms=lars&days_back=10&releases=53
,
Jul 1 2016
,
Jul 6 2016
|
||||
►
Sign in to add a comment |
||||
Comment 1 by aashuto...@chromium.org
, May 24 2016